
During the downtime it received new rear shocks (OEM replicas from PM), new tapered roller steering head bearings, new fuel lines and filters, and a complete front brake job. I found a shop in Denver called American Industrial Brake, that does all the same stuff VintageBrake does for a lot less money and a lot less time. They turned the drum, relined the shoes with modern material, and arced the shoes in. I also picked up a set of new sealed bearings for the front wheel and put those in. Oh, and I also fixed the neutral switch. It had been on all the time, which turned out to be caused by a pinched wire. DPO had gotten the lead wire from the neutral switch caught behind the stator, and when he tightened the screws down he cut through the insulation, resulting in a short and the light being on all the time. All good now though.
The bike started on the third kick and quickly settled into its usual 1500 rpm idle. So out it went for a test run. I need to go one size richer on the main jets, but otherwise it's running great. The front brake still needs to be adjusted properly (I'll have to get a helper for that) but it's already better than it was. And there's no more headshake! Amazing what having all of your bearing races can do for handling.
Here's a photo from today:

When I pulled into my driveway, I smelled fuel however. The carbs appeared to be leaking. It didn't take long to discover the cause:

Oops.

It's great to have the bike back! Nothing like the sound of a two stroke street bike.

Debby